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Back on the Road!

Laxdad32

Contributor
New Member
Joined
Feb 26, 2017
Messages
63
Loc.
Fort Morgan, CO
Been gone from the forums for a long time. Life went a few different directions, but I am finally back to my Bronco's. After a few weekends of work, I am excited that I got my 75 out on the road for the first time in 15 years! Still have a few more minor issues to address, and then see if it is ready for the market.
Bronco.JPG
 

LUBr LuvR

Contributor
Bronco Guru
Joined
Dec 31, 2015
Messages
2,076
Looks great, and must be an even better feeling for you. Bronco looks happy to see the light of day. Congrats!
 
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Laxdad32

Laxdad32

Contributor
New Member
Joined
Feb 26, 2017
Messages
63
Loc.
Fort Morgan, CO
New 235/75 R15 tires, got some coolant leaks fixed, new plugs and wires, and a new heater valve. Getting closer. Started having a slight misfire, and sounds like a lifter tic, so will be looking into that this weekend. Any advice on valve train diagnostics and repair?
 

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blade

Contributor
Maker of sharp things
Joined
May 13, 2020
Messages
172
Loc.
Santa Fe
Pull the valve covers and look everything over. My 74 was parked for a long time and had a dead cylinder. When I removed the valve cover I found a pushrod with the ball on the end smashed flat. I guess the valve was stuck and it hammered it.
 
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Laxdad32

Laxdad32

Contributor
New Member
Joined
Feb 26, 2017
Messages
63
Loc.
Fort Morgan, CO
Pull the valve covers and look everything over. My 74 was parked for a long time and had a dead cylinder. When I removed the valve cover I found a pushrod with the ball on the end smashed flat. I guess the valve was stuck and it hammered it.
I was planning on pulling valve covers this weekend, hoping it will be something simple. I know sitting for that long causes some issues, for sure.
 
Joined
Dec 30, 2021
Messages
12
glad to see another bronco on the road again, I went thru the same with my ' 74 . It stayed in storage for 8 yrs. and I finally pulled it out and started its transition to life again, Marvel mystery oil is the key when you get those valve covers off, just soak everything down push rods, springs, lifters and let it soak, then when you start getting into the tic problem it will be easier to pull everything apart and inspect, sometimes the oil will help free up a problem from setting up, also, watch for scale in your gas tank, I had to pull both tanks and chemical steam them, must have went thru 5 sets of inline fuel filters before I saw what it was, burn non-ethanol gasoline as well and yes I put a capfull of Marvel Mystery oil in my gas tank at every fill up, that stuff is great, good luck and good to see you on the road with her again,
 
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Laxdad32

Laxdad32

Contributor
New Member
Joined
Feb 26, 2017
Messages
63
Loc.
Fort Morgan, CO
Well, figured out the miss and the tic. 2 rockers turned and not pushing on the valves. Pulled rocker arms, inspected pushrods, re-assembled, set torque on rocker nuts per ford procedure, started her up, and both rockers jumping around and popped off valves again. Rockers are very loose on valve and pushrod, thinking collapsed lifters? Didn't really want to pull intake manifold, but I guess that's next. Oh the joys of working on stuff that has sat for so long lmao
 

eb-nutt1

Sr. Member
Joined
Apr 17, 2006
Messages
636
Could be the rocker studs have pulled out heads...check that before removing the intake.

Brian
 
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Laxdad32

Laxdad32

Contributor
New Member
Joined
Feb 26, 2017
Messages
63
Loc.
Fort Morgan, CO
Could be the rocker studs have pulled out heads...check that before removing the intake.

Brian
Looks like a couple studs have pulled out, 3/16" to 1/4" further than the rest. Is there any fix other than pulling heads and taking to a machine shop to fix? Also, what would cause this on a completely stock 50k mileage engine?
 

bulletpruf

Contributor
Full Member
Joined
Mar 31, 2019
Messages
469
Loc.
San Antonio, TX
Looks like a couple studs have pulled out, 3/16" to 1/4" further than the rest. Is there any fix other than pulling heads and taking to a machine shop to fix? Also, what would cause this on a completely stock 50k mileage engine?

That's a beauty!

As for the studs, that engine should have pressed-in studs so about the only think I know to do is to remove the head and bring it to a machine shop, where they would either drill a hole through the boss and stud and pin it in place or install screw-in rocker studs.

You can pin it yourself without removing the head, but that every time I try to do something like that, I regret it almost immediately and vow to never do it again. Shouldn't take you more than 45 minutes or so to remove a cylinder head.

Here's a hack job - WARNING - SHIVVERLAY CONTENT -

Good luck with it.

Scott
 

eb-nutt1

Sr. Member
Joined
Apr 17, 2006
Messages
636
My dad fixed a boatload during his automotive career(45+ years, Ford, Chrysler cert tech) by pulling the old studs, and driving in new studs with red loctite applied on the bases...the studs pulled out because the valves probably stuck...the press in studs were a common issue on mid 70's ford.

Brian
 

sprdv1

Contributor
REBEL
Joined
Mar 8, 2007
Messages
81,983
Well, figured out the miss and the tic. 2 rockers turned and not pushing on the valves. Pulled rocker arms, inspected pushrods, re-assembled, set torque on rocker nuts per ford procedure, started her up, and both rockers jumping around and popped off valves again. Rockers are very loose on valve and pushrod, thinking collapsed lifters? Didn't really want to pull intake manifold, but I guess that's next. Oh the joys of working on stuff that has sat for so long lmao

yes sir, lots of kinks to work out
 
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