Ha, that didn’t age well. 3500 miles in since may and possum was doing great until I decided to go to Good Evening Ranch for a weekend of wheeling earlier this month. Tough drive for possum being nothing but hills and started smelling coolant on the long grades with keeping my foot into it to try and maintain speed. Started losing 7/8 cylinders when on the long hills which turned into random ignition cuts and it not wanting to idle and eventually lost everything while in town. Dad who was following with a truck and trailer and his bronco ran to the local parts store and picked up a new cap, rotor, points and condenser. Replaced everything and no change until I jumped up and grabbed the cap and it suddenly started running fine.
We ended up zip tieing the cap to one side at an angle and bandaided it the hr or so I had left. While looking at it after taking a break and eating dinner, dad went to adjust points and found he couldn’t even adjust the points because the breaker plate kept moving and upon further looking at it, it was work smack out. Called up autozone not 10 mins before they closed and they had a distributor on order which showed up before 830 in the morning. Everything went well and super impressed with how the truck did, but on the way home the temp started fluctuating and a weird “squeak” would develop under change in the throttle, not rpm related but where you were at such as 1/4 or 1/2 or full throttle. Made it home and found a couple problems but pretty sure I blew a headgasket with such a hard drive, which no big deal to throw headgaskets on, but did an oil change before I left and found a large amount of shavings that I don’t like and I assume it to be a wiped cam.
After pondering on that and weighing options I figured I jumped to conclusions assuming the worst but I’m afraid to say I don’t think so. Verified the headgasket and either way that much metal is not good. Possum has been sitting for about 2 weeks and i finally decided to dive into it again over the winter and re-do the interior, wiring and eventually put a motor in. Made a deal on a 385hp 351w crate engine my grandad has had for about 15 years. Anyways here’s some wheeling pics and progress of todays tear down